资料介绍:
M01 Dog overrun 0001
Details When returning to the reference position, the near-point detection limit switch did not stop over
the dog, but overran the dog.
Remedy - Increase the length of the near-point dog.
- Reduce the reference position return speed.
M01 Some ax does not pass Z phase 0002
Details One of the axes did not pass the Z-phase during the initial reference position return after the
power was turned ON.
Remedy - Move the detector one rotation or more in the opposite direction of the reference position,
and repeat reference position return.
M01 R-pnt direction illegal 0003
Details When manually returning to the reference position, the return direction differs from the axis
movement direction selected with the AXIS SELECTION key.
Remedy - The selection of the AXIS SELECTION key's +/- direction is incorrect. The error is canceled
by feeding the axis in the correct direction.
M01 External interlock axis exists 0004
Details The external interlock function has activated (the input signal is "OFF") and one of the axes
has entered the interlock state.
Remedy - As the interlock function has activated, release it before resuming operation.
- Correct the sequence on the machine side.
- Check for any broken wires in the "interlock" signal line.
M01 Internal interlock axis exists 0005
Details The internal interlock state has been entered.
The absolute position detector axis has been removed.
A command for the manual/automatic simultaneous valid axis was issued from the automatic
mode.
The manual speed command was issued while the "tool length measurement 1" signal is ON.
Remedy - The servo OFF function is valid, so release it first.
- An axis that can be removed has been issued, so perform the correct operations.
- The command is issued in the same direction as the direction where manual skip turned ON,
so perform the correct operations.
- During the manual/automatic simultaneous mode, the axis commanded in the automatic
mode became the manual operation axis. Turn OFF the "manual/automatic valid" signal for
the commanded axis.
- Turn ON the power again, and perform absolute position initialization.
- Turn OFF the "tool length measurement 1" signal to start the program by the manual speed
command.
M01 H/W stroke end axis exists 0006
Details The stroke end function has activated (the input signal is "OFF") and one of the axes is in the
stroke end status.
Remedy - Move the machine manually.
- Check for any broken wires in the "stroke end" signal line.
- Check for any limit switch failure.
M01 S/W stroke end axis exists 0007
Details The stored stroke limit I, II, IIB or IB function has activated.
Remedy - Move the machine manually.
- Correct any setting error of the parameters for the stored stroke limit.
模块 A6ADP-1MC16D
制动器接头 MR-BKCN
编码器电缆 MR-JCCBL30M-L
电磁制动器用电缆 MR-BKS2CBL03M-A1-L
PLC FX2N-128MR-ES/UL
视频输入单元 GT16M-V4
PLC FX1S-20MR-D
编码器电缆 MR-JCCBL10M-H
多路转换模块 A60MX
伺服电机 HC-MFS73B
伺服放大器 MR-J3-20B
PLC FX2N-80MS
存储卡 FX-EEPROM-8
PLC FX2N-16MR-ES/UL
PLC FX3U-16MT/DSS
监视电缆 MR-J3CN6CBL1M
可编程控制器 FX1N-14MR-001
伺服驱动器 MR-J2S-30KB4
嵌入型I/O模块 AJ65MBTL1N-32D
PLC FX3U-80MT/DSS
PLC FX2N-64MR-D
伺服电机 HC-MFS13D
伺服控制器 MR-J2S-11KB4
编码器电缆 MR-JCCBL5M-L
伺服电机电源用电缆 MR-PWS2CBL03M-A1-L
PLC FX1S-20MR-DS
PLC FX3G-14MT/ES-A
可编程控制器 FX1N-60MT-001
GT16触摸屏 GT1695M-XTBA
存储卡 FX-EEPROM-4